01-13-2007, 08:55 PM
This morning we took the robot prototype for a short test drive again.
We worked on getting the voltage to every motor the same so all wheels would spin at the same speed and at the same joystick axis value. Several victors were replaced and caliberated.
The rest of the gears were cut down to size by AJ.
Some people worked on ways to impliment Mr. Frank's arm idea into our robot.
The VEX team continued to build work on their scale robots.
We worked on getting the voltage to every motor the same so all wheels would spin at the same speed and at the same joystick axis value. Several victors were replaced and caliberated.
The rest of the gears were cut down to size by AJ.
Some people worked on ways to impliment Mr. Frank's arm idea into our robot.
The VEX team continued to build work on their scale robots.